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Heathkit IG-42 Signal Generator Restoration – Part 2

 

Heathkit IG-42 Signal Generator Restoration – Part 2

Electrolytic Can Capacitor Re-stuffing

Next on the repair plan is to pull the 3-section electrolytic can capacitor, and re-stuff it with modern electrolytic capacitors.  This will ensure reliable operation for decades into the future, while preserving the looks of the old equipment.  I unsoldered the two resistors, the .05 uf capacitor and the various wires from the terminals of the can, being careful to note what each terminal had for connections.  Once that was done, I was able to unscrew the two screws holding the can to the chassis, and remove the can.

 

 
Electrolytic Can Capacitor removed from chassis

The can bracket lifted off, after un-twisting the four tabs on the can.

I worked for about a half hour, attempting to uncrimp the edge of the aluminum can from the bottom.  I tried a pocket knife and a small screwdriver, but I got nowhere in that endeavor.  Finally, I changed the plan and decided to cut the bottom off by grinding on the bottom edge until the steel ring was exposed.  The plan is to use an epoxy to glue it back together, rather than re-crimping the edge.

 
Dremel cutting wheel used to grind bottom edge off

 

Bottom edge ground off, exposing the steel ring underneath.

Once the edge was ground down I was able to simply lift the steel ring off.

 
Steel ring removed

With the steel ring out of the way, I applied hot air with an embossing gun all over the outside case of the capacitor.  I stopped every thirty seconds or so, pulling gently on the terminals to see if the inside would pull out.  After a couple of minutes, they did. (Note** Be careful doing this, as you can pull the terminals right out of the bottom of the capacitor if you apply too much pressure.  The heat is to soften the tar inside the can, so it will let go of the parts inside.)

 
Capacitor guts exposed

Next, I unrolled the foil and paper from the bottom of the capacitor.  This one was very dry, whereas others I have done have still had some liquid electrolyte wetting the paper.  So this one was in pretty bad shape.

 

 
Unrolling the paper and foil layers

When I got near the end of the roll, I started running into the three terminals that connect to the capacitor sections.  I just kept unrolling until all the paper and foil were off.

 
All paper and foil removed.

I cleaned the inside of the can out with some mineral spirits and brake cleaner.  It probably wasn’t necessary, but I like it clean.

 
Clean can

Next, I prepared three modern electrolytic capacitors by soldering their negative leads together to form one pigtail, and arranging them such that they would exit the can in roughly the same positions as the original values.

 
Modern electrolytic capacitors bundled together.

Then I drilled four small holes for the leads to exit the top, placing them near the terminals where they would attach. The leads cannot be soldered to the terminals on the underside, because that part of the terminal is aluminum, and won’t accept solder.  So I just cut the terminals on that side down short and bent them over for some mechanical strength.

 
Lead holes drilled

I should have drilled the holes a little closer to the center, as the leads are a little close to the attaching hardware where I placed them.  There is still enough clearance so that they won’t short to ground, but it would have been better to have more.

The capacitors were placed inside the can, and their leads fed through the four holes.  The ground lead will attach to one of the twist locks when the mounting ring is reattached.

 
New caps in can

Next, the bottom of the cap was glued back into place, with a two part epoxy to hold it.  I clamped everything together and left it overnight to harden.

 
Gluing the bottom to the can

I used my dremel to grind away the excess epoxy on the outside.  This is before cleaning the assembly off.

 
Epoxy ground off.

Then I soldered the leads to their correct terminals, and the ground lead to the steel ring.

 
Completed assembly

Finally, I mounted the can back to the chassis, and reattached the various resistors, capacitors and leads to the terminals they had been removed from.

 
Can mounted back into chassis

Here is a view of the newly re-stuffed can from the top.

 
“New” electrolytic can capacitor in place

 Migrated Comments:

One Response to “Heathkit IG-42 Signal Generator Restoration – Part 2”

  1. Steven Read Says:

    You did it a lot neater than I did. About 45 years ago I replaced a multi-segment electrolytic in a DX-100 but instead just wrapped the replacement capacitors in electrical tape & created “lugs” from banana plugs. It was not one of my better efforts but it worked.

     

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